The 4A-GE Midget gets closer

Having to use up a load of holiday I’ve another week off so can spend some time on the 4AGE Midget.

With a spare hour on Saturday I managed to attend to the wings. Being GRP wings I didn’t take them to the gel coat and sure enough a couple of areas reacted to the primer on one wing. A rub down and a spray with a barrier coat paint had them ready for priming.  Monday was a bit cold but I was able to prime and top coat the wings an bonnet and rectify the boot lid.

Fitting the bonnet was easier than I expected but the rear edge was rather low. I was expecting to have to shim out the hinge but after a lot of searching I found a reference to placing blocks of wood under the V of the hinge and then gently forcing the bonnet down. Sure enough that raised the rear of the bonnet to the top of the scuttle.

You can just make out that the rear of the bonnet is below the top of the bulkhead.
You can just make out that the rear of the bonnet is below the top of the bulkhead.

Having had to move the car earlier to make space in the shed, it was frustrating that it wasn’t running as well as it had before. If revved it would die at 3000rpm and just wouldn’t run. I’m rather ashamed to say that the problem was a lack of fuel and as soon as I put a gallon in the tank the fuel gauge moved from empty and it started to behave.

Day 2 of the holiday and I’m winging it today.  The wings are GRP and I recall that they weren’t a brilliant fit when I got the car. Therefore I’m not expecting miracles and will have to accept that I can only do so much with them.  Come lunchtime and I have the offside wing fitted and come mid afternoon both wings are bolted into place and aligned the best that I can. The offside wing is slightly shorter than the bonnet and this is something I spotted on a couple of cars at Silverstone a few years ago.

wings-fitted

After a coffee break it was on to the wiring ( a job I really do like ) and time to fit some new headlights. With the headlights fitted it was time to test that they worked. Battery connected, ignition on and we have dipped beam but no full beam. The full beam relay didn’t even click so that was swapped with the known working dipped beam one but still no joy.  For some reason I went straight to removing the fuse & relay box and the cause was obvious, some muppet hadn’t fitted the relay signal earth lead. Ten minutes and one lead later and we have working main beams.

bright-eyes

Just as I was turning the car round on the gravel drive my dear wife  arrived home to witness some hooligan behaviour 🙂

Time for an Old Crafty Hen to celebrate…